How to duplicate a 650-hp 383 small-block for around $4,900 |
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By David Vizard The goal for any hot rodder on a budget (that’s almost all of us, right?) is having the most for the least. We are looking for inexpensive simplicity, practicality and drivability. Well here it is! Most project engines have a goal of doing a one-time build and (hopefully) meeting the required target parameters. This motor was a little different in that it was used to test products along the way. It started life as a dyno mule and will remain so after this project is done. Because of this, you will see parts and procedures that were deemed necessary for a hard-working dyno mule that you won’t need to duplicate this build at home. This will be mostly evident in the bottom end.
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The Block
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In line with the old adage that there is no substitute for cubes, our project engine used a Scat 9000 series cast steel crank (part No. 9-350-3750-6000) to stretch capacity from 350 to 383 inches. This crank is designed to internally balance with Scat’s inexpensive “I” beam 4340 alloy steel cap screw six-inch rods. If you intend to follow our build this is what you should use. The test motor, however, was to be used as a cam test engine later and would be turned up to 7,700 rpm. For this reason what you see in our engine is an internally balanced (with four slugs of Mallory metal) 9000-series crank and a set of Scat’s “H” beam rods. Pistons were from Ross. These were chosen because they are cost-effective and amongst the lighter off-the-shelf pistons. This is important when a 3.75-inch stroker crank such as the Scat item is used. If the pistons are a little overweight then the balance job gets expensive. Because nitrous was to be used to put a thick layer of frosting on the cake, the pistons received a thermal barrier coating from Calico. For us this is a safety measure as it makes the pistons near bullet-proof against detonation. This won’t be a problem with the 650hp we make here, but down the road this engine will be subjected to nitrous loads that push the limit. As a product of results from my own extensive dyno testing, a Total Seal ring set with the gapless top ring was chosen to compliment the Ross pistons. Lubrication of the bottom end was handled by a pump and pan from PBM. This company is “trade only” but a call will get you their nearest dealer. It’s worth the effort because the quality is up and the prices are down. |
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![]() We used Scats H-Beam rods for a mule that was to a lot of hard work. Replicating this build for the street will only require the 9000-series crank and lighter 4340 rods seen here. ![]() An economically-priced regular oil pump from PBM was used <======= together with a PBM pan.=====> This inexpensive piece features a surge baffle and an oil scraper. With a 383 crank, the scraper needed trimming about 0.030 where the rods pass it. |
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A gapless top ring set from Total Seal produced the low leak-down figures sought after.
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The original intent here was to build a nitrous engine using one of Nitrous Express’s basic plate systems. When I called the boss, Mike Wood, about a system, he asked if I would like to use one of their new line of Nitrous Cams. I have to admit a nitrous company in the cam business could make a pro engine builder a little nervous and I voiced this opinion. It turns out that though Nitrous Express handles the vital aspect of spec’ing out the valve opening/closing events to suit whatever degree of nitrous used, they draw on race experience and the expertise of a number of top cam companies to come up with what proved, in this instance, a highly functional combination. In this context “functional combination” also means good dynamics. I knew Nitrous Express nitrous systems worked great because I had a fair amount of dyno testing under my belt with such, but Nitrous Express cams were another deal, so to be included in the build, whatever cam selected would have to be tested against a known functional cam. Most people are under the illusion that if a cam worked optimally in their 350 it will do the same in a 383. This is not so. The plan here was to go with a hydraulic flat-tappet cam. However, the test would be done against a solid flat-tappet cam having the same opening duration as measured at the lash. In other words, a true comparison. You may well ask, “why should the NX hydraulic cam be pitted against a solid?” The answer is this will also give us some idea of the quality of the dynamics (and consequently the power producing capability) of the combination they intend us to use. Whether we like it on not, hydraulic cams can run into problems associated with lifter pump-up and collapse. Tests with hydraulic cams run with solid lifters carefully lashed at 0.006 to 0.008 can show as much as 20hp more at the top end while usually giving away some 10 to maybe 15 lbs.-ft. at the bottom end. A little lifter collapse at low speed can be good but, at high speed, it needs to be minimized if top end output is to be maximized. With this in mind, the project then became a cam test project. To be sure the best is achieved from a cam test, the
cam timing needs to be optimized for each cam and the quickest way to
establish the optimal position in the engine is to use
As can
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| For a valve train it is important that the parts are all compatible as it must operate as a system. For small-block Chevy and Ford applications, he NX cams (as with their LS1/6 grinds) absolutely must be used with a |
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| beehive spring. This spring is so much more effective than a regular parallel-wound spring that it allows less poundage to get the job done. The spring used delivered 110 lbs. on the seat and, at 0.520 lift, 270lbs. over the nose. NX recommended several rockers; the ones used were 1.6/1 ratio and sourced from Crane. Pushrods were Comp Cams Magnums and the lifters, matched to the cam, were supplied with the NX cam. | |||||
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The heads selected for our project motor were from
Canfield. There were several reasons for this. First, the 195cc port
volume gave the desired mean port area for a
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| Fig 2. here are the figures produced by the 195cc port Canfield heads. Since the valves will only be lifted about 0.520, what they flow above that is academic. | The beehive springs used on the heads were an important part of the valve train equation. Make a change here and you will most likely watch 1,000 rpm disappear off the top end. | ||||
Good
out-of-the-box flow, near-ideal port volume and good swirl promised and
delivered results from the Canfield heads. |
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| A functional valve train is very much a case of systems engineering. This combination of parts worked extremely well. | |||||
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Based on previous experience, a Brodix Hi-Velocity intake manifold was used. This put on a good show with a 270 degree cam and an even better showing with one of 280. Here we are using cams of some 288 degrees of off-the-seat duration. This, with the 383 cubes displacement, looked like it might just be enough cam to warrant going to the bigger runners of the Brodix manifold compared to say a Victor Jr. As it turned out, a Victor Jr., which with a 1-inch spacer, brought it up to near the same height as the Brodix manifold, produced virtually identical results, so you get to take your pick. The Nitrous system used was a basic NX plate system (part No. 30040-10). This kit is rated to produce between 50 and 300 hp depending on the jets installed. The plan here was to jet for about 150 -175 hp increase depending on what was seen as the baseline before injection took place. The carburetion was a carry-over from the earlier intake manifold tests. Both a 750 Road Demon and an 850 Race Demon were tried. The 850 showed no low-speed loss at 2,500 rpm but did net about 8 extra horses up at the top end. |
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After breaking in the motor on the solid flat-tappet cam, some 30 pulls were made to optimize carb jetting with each of the two carbs used. Based on results, the 850 was chosen. However, be aware that a Race Demon is more money than the Road Demon. If dollars are a real issue, the 650-hp target can still be met with a Road Demon. At this point, we were ready to do the cam evaluation. With the lash checked and set for the solid flat-tappet, a number of pulls were conducted with small changes in cam timing made every half dozen or so runs. This established the optimal timing of the baseline cam. Once this was done a shot of nitrous was administered. Here is where the weather once again caused problems. These tests were run in January in freezing weather. Even though a bottle heater was used, the low temperatures in the dyno cell prevented the nitrous bottle from holding its pressure. The result was a pressure that dropped from 950 psi to under 650 in almost no time flat. As a result, it was only possible to make spot checks of the extra power delivered by the NX nitrous system. At 3,500 rpm the 100hp jets delivered 104 hp. At 5,500, the increase was 98hp. |
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For the next test session the 288/288 solid-lifter cam was replaced with the NX Nitrous cam. When ordering a cam from NX, you can specify whether you want the cam to favor output with the nitrous in operation or not. In this instance it was decided too bias the cam spec only marginally to the nitrous operation mode. This would then give the best output during normal day-to-day operation. This decision was made because previous tests with 350s had shown that the 650-hp target could be made relatively easily with the right parts combination. Concern over whether the NX cam would deliver proved groundless. As the chart (Fig. 3) shows, the NX cam delivered in fine style. It looked to be among the best flat-tappet hydraulic cam and valve train combinations I have tested. Although an improvement in low-speed output was expected, as soon as the numbers came off the dyno I had to question why the NX cam was so good at the top end. The dyno numbers are the result of seven runs with the best and worst thrown out and the remaining five averaged out. These numbers showed the NX cam actually made 11 hp more at peak power and, at 6,700 was still 2-3hp up on the solid-lifter cam. To see just where this cam and valve train might let go, the engine was turned to 7,000 rpm where the valve train just purred. That’s a level way above what is normally expected of a hydraulic cam. A brief foray to 7,200 also showed no sign of any loss of valve train control. At this point our project engine was proving itself to be truly streetable. With the vacuum advance hooked up, the combination of compression, cam, carb and ignition allowed a very smooth 650 rpm idle. As for output, we’re looking at a very respectable 475 lbs.-ft. of torque and a little over 485 horses. All this comes with about 370 lbs.-ft. at 1,900 rpm. Now it’s time to put the nitrous to it and see how the numbers change. The 100-hp jets for the NX system were first to be tried. Again the spot shot technique had to be used because of the still freezing weather. At about 3,500 this netted some 108hp increase. At 5,800 104 extra hp was realized and peak power climbed to 590 hp. The highest torque figure seen was at about 3,900 and showed 660 lbs-ft. At this point it was decided to go straight to 76 and 55 jets for the 175hp needed to attain the target figure. With the bottle up to pressure after about 40 minutes of heating, it was realized we had one shot at this before having to take the engine off the dyno for the next project. In about the 3-4 second period available before the bottle pressure plummeted, the two numbers observed on our DTS dyno were 657hp and 772 lbs.-ft. of torque. That kind of output will give you really wicked street performance. If you shop around for the parts you can replicate this motor, less the exhaust system but with everything else including plugs and oil, for under $4,900. If you do not want to assemble the motor yourself then add about another $1,000 for a competent pro to do that for you. |
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Featured Article in August 2004 Popular Hot Rodding |
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The block for this motor has been a mule motor block for me since 1982 and
was most recently used for our Performer rpm tests.
(See
“The Street Game,” June 2004.) As a result, it has been progressively
refined. It has had all the oil galleys “ported” to cut pressure losses
from the pump to the bearings. The entire valley has been ground smooth
and painted with electric armature enamel to enhance oil drain back and to
look good in photos. Also, stand pipes have been installed to direct oil
return to the ends of the block. All this is optional but not necessary
for what we are doing here. What is necessary is that you source a block
from a company competent to select and machine a block that is up to par.
Essential machining includes boring and deck plate honing, align hone the
mains and deck the block so the pistons come out by 0.005 to maximize
quench and enhance resistance to detonation.

Consider this
option, but our internally-balanced Scat cast steel crank was given the
once over with emery rolls and then coated with an oil-dispersant Teflon
coating.

an adjustable belt
drive. A regular timing chain set will replicate the finished results and,
up to this point, the intent had been to use a cost effective PBM-sourced
timing chain set. The two cams to be compared had the lift/duration specs
shown in the chart Fig. 1
be seen, the cams
are very similar. If the high-speed dynamics of the entire hydraulic cam
and valve train system are up to snuff , then it should produce close
to the same top-end power as the solid. At low speed, there is time for
the hydraulic lifter to collapse so both the intake and exhaust valves
close sooner. This shortens the duration and advances the timing. Both
these event changes are good for increased low end. At the end of the day,
most hydraulics show better results at low speed than a solid of equal
duration. Where they normally fail is that they don’t make the top-end
output and they suffer dynamic problems which limits their rpm potential.
This test, as planned, should put the NX-sourced cam through its paces in
no mean fashion.
383-inch engine
expected to make peak power at around 5,800 rpm. Secondly, flow testing
(Fig 2) showed that these heads, out of the box, flow very well up to
about the maximum valve lift (0.520) that was to be used. Third,
the chambers are
CNC-finished for a consistent CR. Last and certainly not the least is that
they are economically-priced and that’s always a good factor for a head
that works well.
Good
out-of-the-box flow, near-ideal port volume and good swirl promised and
delivered results from the Canfield heads.